I have the feeling of a slow reaction or small lag between Tx stick movement and the copter compared with other boards like Arducopter, FY90, KK, etc).
In this video you can see what I mean. I keep the copter with the hand free of rotation:
Is that the normal functioning? (I´m using futaba FP8 and Rx = r6208sb)
I´ve tryed to change followings parameters without success:
Tilt_Angle_P (default=60) moved up to 120 in steps (it wobbles at high values)
Tilt_Angle_F (default = 0.25). Moved up to 0.5. This param seems to improve a bith the reaction
Tilt_Rate_P (default=0) up to 100.
Any Idea?
Angel