Hi, I recently puchased my second AQ board and wanted to build a new quad based on the quadframe mediumweight quad with alu arms, so less problems with aligning the motors
Motors are are sunnysky X2212-13 980 Kv
Turnigy plush 30A ESC Simonk flashed
5000Mah 3S batt
Carbon props 10 x 4,5
I also gave in to a new Frsky taranis
ESC are calibrated, props balanced, did AQ static and dynamics cals,using standard AQ quadX motormix, ... but I just can't get the quad tuned. The problem is that the motors are pulsing a lot and it keeps jumping up and down.
I used to fly this board with the same ASC ona DIY frame with KDA 22-20L motors which flew allmost perfect.
To get the oscillations/pulsing out of the motors I increased tilt rate D to about 8300. It helps is bit (not much) but I'm a little bit afraid togo higher.
Do you guys have any more suggestions?
Included is a log of two short attempts of level flight.