mhhh... maybe i've got too much vibrations... i'm flying with CFK el-cheapo rctimer CF props... not BALANCED (i just discovered that my balancer is out of balance by itself... so no make sense to balance with that tool...).
say that. i have 6 esc32, all the 6 are reflashed with 1.4 version and no tuned parameters, defaults was used. Only one question... the "control mode" of the esc is a parameter used by AQ or just open-loop so no matter what parameter i insert ? i ask that, because just after the flashing and connecting with GC 1.0.5 the control mode shows RPM (instead of openloop) if i change in openloop, then close GC, open again and reconnected to the ESC, the values is back to RPM... i don't know if it is normal. maybe that cause problems...
the props are all the same sizes and motors is all the same brand and type (obviuosly). triple checked that the propellers match with the sense of rotation of motors, and all 6 motors pulls air in the same direction..(maybe stupid... but i checked also that...). Said that, i really don't understand where the unbalance came from...
maybe the two motors you see with no clipping is because in the mixer the front and the rear motors is setted at 70%, so the output was lower that the others...
i still pointing my attention to the after calibration check file... i don't know if any of you have tried this procedure (http://autoquad.org/wiki/wiki/autoquad- ... on-result/) ... but for me, revealed that the sensors drift a little over temperature and the gyro seems not to be aligned at all...
i'm scratching my head since the beginning of my aq adventures, it's not easy to find out problems...