so i finished my second AQ build, it´s a Hex+, AUW 2600g, Roxxy 2827/35, eProp 10x5, 4s2600, Flyduino Carbonframe, RcTimer 30A ESC /SimonK flashed, Spektrum reciever.
First of all i forgot to set trottle value for 2 motors and one for roll in the mixingtable, second i forgot sponge on the baro but thats not the point, it flyes awsome. Of course fixed that for the log postet in this post!
PID all like they come in the r37 and yes i can not compile so i use r37 for AQ v1 at a AQ v2 board. Not long flighttimes, you are right
but thats also not the point. Remember: it flyes awsome!
So what´s the point: it fliew horrible with the motor_mixing_table i took from the Wiki, jumped up´n down, loud, horrible motornoise, and no altitude holding (at ph and also not in manual).
I went back to the motor_mixing theory which made my AQ Quad fly so wow and decidet to do something like that.
It is now dark so no flightvideo.
thats how a log should look a like, thought.
remember: it flyes ..........
So please someone more inteligent than me tell me what i stumbled into?
Marcus