Hi, all.
I met a serious problem with my AQ6.
My components included:
1.Motors were 3110 700kv and Props were 10x55.
2.ESC was Q-brain 4-in-1 25A.
3.My RC was Spektrum DX7s with AR8000 receiver.
4.To overcome vertical altitude override, the FACTOR_THROTTLE was changed to 0.75. The other settings were default.
5.My frame was 550mm Quad-X.
In the position-hold mode (GPS was 3D-fixed), when the throttle was middle, my AQ6 flied up and down.
During the tests, no strong wind existed.
The video was here ().
I checked the log file ().
Everything looked well as Figs.1 and 2 shown.
I cannot find out the problem.
Please help me.
Thanks for help.