I've come to the part of the dynamic cal but before I do the dance I want to check that the hexa flies accordingly. (should be able to do this)
But I have a problem.
During the initial test I wanted to check that the hexa responds to the tx input. Pitch and roll are ok but I have no response on yaw. After a few seconds the hex start turning randomly without tx input.
All channels respond in the GCS.
I checked and rechecked all settings and connections but can't seem to find the problem.
I also loaded two different motor mixes but problem stays the same.
Any suggestions?
I'm using a hexa x setup with simonk ESC's.
Here is my mixing table.
M3 is left front
M2 is left
M1 is left aft
M9 is right front
M8 is right
M7 is right aft