Hi All,
i just finish my quad with following configuration :
- AQv2 with fw Version v6.6.1 stable (b1036)
- simonk fw F-20 ESC (put on under the motors, change cable using small coax shielded audio cable, twisted the power cable + 1K ohm resistor)
- MT3506 motors + 12x4.5 props
- Hott2mavlink using Jdrone board (using 2K2 ohm resistor on data cable to AQ)----> it works very well
- bluetooth
- PPM GR-12 receiver (using 2k2 ohm resistor on data cable to AQ)
- alexmos Gimbal controller (not using it yet)
All power cable was twisted
All props is balance
The result is :
- it cannot fly even the trottle is half
- the motors is not stable gas (like motorcross start race), its might the ESC is not syncronizing with FC ?
next action :
- I change the motors with Sunnysky X2216-11 with 10x4.5 props
the result is still the same.
is any something I missing the step ?
is it any difference setting the simonk ESC and ESC32 ? or any special firmware for simonk ESC ?
I appreciate any comment.
Thanks,
John