Hi,
I have managed to go through the calibration and calculation. And now I wanted to perform some checks before the maiden flight, but even when the copter is armed (green led on) my motors are remaining idle. I have tried several values for MOT_START (from 950 up to 1150) but could not solve the issue.
I am running Flyduino ESC with SimonK firmware, my ESCs have been calibrated and are running smooth when connected directly to the throttle channel of an RX.
Anybody an idea what I should do to get the things running? I had never such issues with MultiWii and I am sure that it is only a little thing which is hindering me of flying my AQ.
Thanks and best regards,
DUKE40