Okay, so, it looks like I cannot test with Turnigy 9X since it doesn't output PPM signal...
Today it was a bit difficult to cause the board to freeze. It only bugged out one or two times out of ten. I was able to record a log where it bugs out really quickly after powering up - please see the attachment.
Also, how would it even be possible for my radio to cause the board to freeze?
Now, I have another proof that my radio indeed works fine. When I was trying to record a log for you, a weird thing happened that has never happened before - the board bugged out, that is it didn't respond to external inputs (moving the copter), but the telemetry was still working! I could also turn the motors on and off, but they wouldn't go above idle RPM, no matter how high the throttle was set or how I would move the copter / any other radio stick. I have recorded this incident with my phone and you can clearly see in the QGC that my radio is working fine! Please listen carefully to the motor sound - they don't react to anything at all. They could only be off or run at idle speed.
If this doesn't prove to you that everything's okay with my radio - I don't know what does.
EDIT: Forgot to attach the LOG file:
- AQ malfinction.LOG
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