- esc32 parameters.jpg (123.29 KiB) Viewed 15772 times
1. First of all the motor doesn't start with default parameter using PWM pulse from autoquad in manual mode. I had to increase start voltage to 2.5v from 1.1v and max period to 30000 from 12000. Do you think its Ok
2. I tried current calibration on linux. but could not do the rpm to voltage calibration in linux as the test simply could not start the motor as motor got disarmed automatically(probably due to same reason as mentioned in 1)
3. I conducted the tests finally in QGC(CL and Rpm to voltage) with max current set at 11A(RCTimer motor has 10A max rating). Used these values and set the ESC in CL RPM mode.
4. I tied the motor to test bench connected the autoquad to it armed it and gave throttle in manual mode. Shook the aq board with hand to see if the motor runs fine. The motor sound is some how not quite correct. I am not sure if motor will keep running in air as it stopped a few times during bench test.
5. Can someone tell what should be timing advance angle for this motor(default is 10). If I Change it will I have to redo the calibration again
6. The motor reaches max current around 80% throttle. The throttle response doesn't seem linear