Hi,
I am starting to play with ESC32 v3, 6S to drive 4006 24poles 380kv motor on 16". When reaching high RPM I had to play with switching frequency and advance to prevent stalling when going full throttle on.
I noticed that removing active braking removed the issue. Any idea why this is related to loosing sync?
Now, I have a system that works with 25° advance and 32kHz switching freq but motor temperature @full throttle is quite hot...
Should I try to lower advance? How to keep motor a bit cooler?